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NTSB

Pilot tuned to wrong frequency causes inflight collision

By NTSB · July 23, 2020 ·

Probable cause: The Extra pilot’s failure to see and avoid the Cessna, which resulted in an in-flight collision. Contributing to the accident was the failure of the Extra pilot to tune his radio to the correct frequency, which resulted in no common traffic advisories being heard or recognized as relevant by either pilot.  

Pilot mistakes service road for taxiway

By NTSB · July 22, 2020 ·

Pilot Error NTSB Accident Report

Probable cause: The pilot’s inadvertent navigation onto a service road instead of a taxiway, which resulted in a collision with a stop sign.

Pilot selects wrong fuel tank for departure

By NTSB · July 21, 2020 ·

Probable cause: The pilot’s selection of the wrong fuel tank for departure, which resulted in fuel starvation and the subsequent total loss of engine power.

Bird hits Cessna 560

By NTSB · July 20, 2020 ·

Animal Encounter NTSB Accident Report

Probable cause: The airplane’s collision with a bird during approach.

River landing goes awry

By NTSB · July 17, 2020 ·

Pilot Error NTSB Accident Report

Probable cause: The pilot’s failure to maintain clearance from trees while maneuvering the airplane at a very low altitude in a confined area while attempting to land on a river.

Worn ignition switch and key leads to fatal unintended engine start

By NTSB · July 16, 2020 ·

Equipment Failure NTSB Accident Report

Probable cause: The undetected wear of the ignition switch and key, which allowed removal of the key from an intermediate position and subsequently led to an unintended engine start-up. Contributing to the undetected wear of the 42-year-old ignition switch was the lack of guidance by the switch manufacturer and airframe manufacturer for procedures to detect lack of integrity between the ignition key and switch.

Student pilot’s improper solo ends in forced landing

By NTSB · July 15, 2020 ·

Probable cause: The student pilot’s improper decision to conduct a solo flight without an endorsement to do so and to perform an off-airport landing based on a perceived performance issue with the airplane. Contributing to the accident was the pilot’s lack of training and overall experience.

Bad approach ends in hitting dock

By NTSB · July 14, 2020 ·

Pilot Error NTSB Accident Report

Probable cause: The pilot’s improper approach over a river, which resulted in a collision with a dock.

Pilot’s reckless low-flight proves fatal

By NTSB · July 13, 2020 ·

Probable cause: The pilot’s intentional low-altitude flight, which resulted in an impact with power lines.

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