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Test flight ends with total loss of engine power

By General Aviation News Staff · May 3, 2025 · 8 Comments

The pilot and his son had recently finished building the Rans S-21.

The accident flight was one of a series of test flights the pilot was performing after making cowling modifications.

After a normal departure, he flew to a test area and was in flight for about 20 minutes. While he was maneuvering at about 700-900 feet above ground level (AGL), the engine made “rough” sounds and vibrated. About 20 seconds later, the propeller seized, and the pilot made a forced landing in a field near Creswell, Oregon.

During the landing roll out, the airplane flipped over and came to rest inverted, damaging the vertical stabilizer.

Investigators conducted a post-accident examination of the wreckage, which included a complete disassembly of the engine.

The UL Power 520T six-cylinder engine was new when installed on the airplane and had amassed a total time of about 55 hours. The pilot noted that for about the last 20 hours of engine operation, the engine monitoring unit showed that the cylinder head temperatures (CHT) in the Nos. 3 and 4 cylinders were high (occasionally the Nos. 2 and 6 cylinders would also be high). In response, he changed to a larger oil cooler and was modifying the cowling to increase airflow.

When investigators removed the cowlings a trace amount of oil on the bottom cowling was noted in the area under the Nos. 2, 4, and 6 cylinders.

Removal of the top spark plugs revealed that all showed signatures consistent with normal operation.

Investigators were unable to rotate the crankshaft by hand using the propeller. It would only rotate a few degrees before binding. Clean, uncontaminated oil was observed at all six rocker box areas.

Removal of the cylinders revealed that the combustion chambers and pistons were undamaged.

Removal of the oil sump drain revealed that the magnetic plug was full with ferrous metal; metal pieces were also found in the oil sump. The oil pump was disassembled and there was metal found inside, with the exception of the bypass spring.
 
Upon applying force to the propeller, the engine would not rotate through. Removal of the pistons revealed that the crankshaft was fractured at a web (crank cheek), just aft of the No. 2 connecting rod journal. The thrust bearing mount was able to move forward and aft.

Disassembly of the crankcase revealed that the six connecting rod journals still had their respective rods and caps attached; all were able to be easily rotated about their respective journals.

The fracture extended through the crank cheek in the area between the No. 2 rod journal and the No. 3 main journal. The fracture surface was relatively shiny and reflective, with a portion of the cheek showing severe deformation damage and heat tinting on the forward face. The preliminary assessment of the fracture surfaces was consistent with a fatigue fracture at the aft radius of the No. 2 rod journal.

The National Transportation Safety Board Materials Laboratory examined the engine crankcase, crankshaft with attached connecting rods and bearings, seven pairs of main bearing halves, two filters, and sectioned oil tube.

The No. 2 rod journal’s aft fracture face displayed crack arrest marks consistent with fatigue cracking, originating from multiple points at the surface of the aft radius.

Circumferential scoring marks were present on the surface of the aft radius, intersecting the fatigue origin area, with the fatigue crack measuring about 1.6 inches. The crack propagated through 30% of the rod journal cross section. The remaining fracture extended axially through the crank cheek between the No. 2 rod journal and the No. 3 main journal. The major portion of the crank cheek fracture exhibited damage consistent with post-fracture mechanical damage. The mating fracture exhibited similar fracture features.

Evidence of superficial cracks at the radii locations was observed in the No. 1 main journal, No. 1 rod journal, No. 2 main journal, and No. 2 rod journal. The remainder of the crankshaft revealed no evidence of cracks at the radii locations.

The bearing shell halves for the No. 2 main journal at the inner surface showed evidence of severe circumferential scoring that exposed the steel core layer, and the inner layers of copper, aluminum, lead, and tin, whereas the inner surface of the remaining main journal bearings showed evidence of moderate circumferential scoring.

Examination of two oil filters (one oil filter was mounted on the engine at the time of the incident; the other oil filter was replaced during the last oil change) revealed that the accordion-like fabric section contained material embedded within them.

Examination of the exterior surfaces of both fabric portions indicated the presence of metallic particles.

Analysis using a handheld alloy analyzer detected metal particles containing aluminum, lead, copper, iron, zinc, nickel, molybdenum, and chromium in varying proportions, consistent with metal from the crankshaft bearing shells.

The specified torque for the propeller flange bolt was 221 foot-pounds (ft-lbs) and it had not been removed since its initial installation. Disassembly of the propeller flange bolt with a wrench revealed that the bolt required less rotational torque to remove than expected and the threads from the disassembled bolt showed no signs of mechanical damage. It was not possible to check the propeller balance due to damage incurred after impact.

The post-accident download of the ECU revealed that the turbocharger pressure and fuel pressure were below operational limits, which the engine manufacturer stated would have resulted in a leaner mixture. In addition, the wide-open throttle RPM was, in certain moments of the flight, below operational limits, which the engine manufacturer stated would result in additional stresses on the piston/crankshaft.

Probable Cause: A total loss of engine power caused by fatigue cracking and fracture of the crankshaft due to severe wear of the bearings.

NTSB Identification: 130455

To download the final report. Click here. This will trigger a PDF download to your device.

This May 2023 accident report is provided by the National Transportation Safety Board. Published as an educational tool, it is intended to help pilots learn from the misfortunes of others.

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Comments

  1. Scott Patterson says

    May 6, 2025 at 12:38 pm

    My report would have been;
    Crankshaft failure due to, manufacturing defect..

    Reply
    • JimH in CA says

      May 6, 2025 at 4:07 pm

      I’m not sure sure…why did the #2 main bearing fail first ?

      Reply
  2. Joseph M. Smokovitz says

    May 6, 2025 at 7:50 am

    Propeller bolt torque of 221 FOOT-POUNDS (ft-lbs)??? I think that value is way too excessive. Perhaps it is meant to be 221 inch/pounds.

    Reply
    • JimH in CA says

      May 6, 2025 at 4:06 pm

      Note that it is the center bolt holding the prop flange to the crankshaft extension, not the 6 prop bolts.! A unique design.

      Reply
  3. James B. Potter says

    May 6, 2025 at 4:56 am

    After only 55 hours of operation? Something’s rotten in Denmark here.
    /J

    Reply
    • Wylbur Wrong says

      May 6, 2025 at 7:16 am

      The NTSB seemed to me to be hinting that the prop was not “balanced” and/or the prop bolts were not torqued to the specified amount — “The specified torque for the propeller flange bolt was 221 foot-pounds (ft-lbs) and it had not been removed since its initial installation. Disassembly of the propeller flange bolt with a wrench revealed that the bolt required less rotational torque to remove than expected and the threads from the disassembled bolt showed no signs of mechanical damage. It was not possible to check the propeller balance due to damage incurred after impact.”

      So they seemed to be indicating, from what I read, that this may have been the cause of the engine damage.

      Reply
      • JimH in CA says

        May 6, 2025 at 8:24 am

        Other items investigated were the 2 oil filters, the current one and a previous one. [ the pilot had saved it but didn’t cut it open].
        Both show a large amount of metal, and should have caused the pilot to ground the aircraft.
        So, my thoughts are that the ‘out of spec’ high power operation of the engine had caused the #2 main bearing to fail, which allowed the crank to flex and fracture.

        More stupid pilot tricks and a ‘Forest Gump’ moment.!

        Reply
    • JimH in CA says

      May 6, 2025 at 8:41 am

      Most machinery, including electronics, follow a ‘bathtub curve’ on failure rate vs time in service.
      The early ‘infant failures’ are due to defective materials , incorrect assembly, or poor operation. Most engines are most prone to fail in the first 100 hours; new, overhauled or extensive work. After that, it is in the ‘useful life’ range. Then after some number of hours it enters the ‘wearout range.
      Fortunately, the wearout range has parts usually show an indication of excessive wear….metal in the oil filter, high oil use, low oil pressure, and others. So it is usually not a catastrophic failure, as an infant failure may be.

      This engine having metal in the oil filter gave a warning of parts failing.!!!

      Reply

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